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Showing content with the highest reputation on 04/21/2025 in Posts

  1. Items in the works: I've got a handful of things still to do short term but the list is finally getting shorter. Firstly the important items learned from the recent Moab trip would be that I need axle limiting straps and a taller spring would be ideal. I want to eliminate the HDPE spacers I've used for years and get an all-spring setup. I may also move the spring perches forward and fabricate new lower shock mounts that will provide more clearance. Still have some research to do on that front. While I was coming through Oregon I took advantage of a sale+no tax+IST coupon to walk out the door with a 12K winch for $260 bucks. Just need to swap over my old 9.5K Smittybilt synthetic rope and figure out where to remote mount the solenoid. The front suspension really isn't terrible, especially given my KYB's are approaching 10 years of age, but my roots in high speed off-road really have me wanting to build a better front end. Long term I have plans to make a LT front setup that should fit the bill very nicely but it'll be a ways off. For now there are a set of motorsport coilover struts that should work with the Nissan suspension components after a few changes. I think the weakest link of the whole front setup is the lower control arm mounts and overall method of stamped sheet metal manufacturing. A set of chromoly tube arms with through-bolt mounts and the motorsport coilover struts would be pretty slick and get me closer to the machine I want. I'm sure there are a few bits I've missed but this should be mostly up to date now. A few pics from the recent Moab trip with @hawairish
    2 points
  2. Speaking from experience you are way better off removing the RMS retainer and re&re the seal on a workbench... Trust me, I did it on the truck and it was a bear getting in, and guess what, it leaks again! I still have to pull my transmission off and do it again... When I swapped motors on my Xterra I was able to polish up the crank a bit with the retainer off, and it was MUCH easier to install it that way. You can use like an old margarine tub or something and cut the side of it out, then put that inside the seal to help it slide over the crankshaft. Use lots of lube when installing it so it doesn't start up dry. Easiest way to post pics is use imgur and then post the link here.
    1 point
  3. Wow!! That rig sure looks alot like the beauty gracing my drive the other day! What a ton of work and such a lovely and practical result!!
    1 point
  4. The rear arms I built years ago got an axle side change to some beefy heims in recent years. I'll start by saying I don't recommend them and will be changing them to Johnny Joints in the near future. They are super high maintenance and started squeaking within a year of install. They're probably fine for a trail toy or someone who just doesn't care about the noise. The performance was impressive but not worth it in the end. I started by media blasting the arms I built to get rid of the damage from DOT liquid de-icer's used in recent years. Then painted everything and applied a healthy layer of anti-seize. I kept the body-side rod ends poly to provide some insulation from noise and vibration and the combo worked well prior to the heims making noise. At this time I made a driveshaft spacer from 6061 AL to allow me to push my axle further back into the center of the wheel arch. Pretty easy job and solved an issue with lifted R50's that most folks don't account for when going higher. At some point during all this I started rehabbing a spare HB233 housing for the eventual rear disc brake setup that I picked up from @hawairish. I had the axle housing media blasted and coated it in POR-15. My OE axle shafts needed to be turned down to fit the WD rotors but later models apparently don't need that modification as the axle flanges were smaller in diameter. All new seals, bearings, rotors, pads and refreshed calipers. When I eventually get the axle done it'll be a short period of down time since I should have everything ready to swap in.
    1 point
  5. I said goodbye to my old set of KM2's on vintage mags and K02's on Tacoma alloys. Picked up a new full set, including a matching spare, of KM3's on some 15x10 AR alloys. With the impending long distance road trip the 8 year old rubber was a liability and it was time for a refresh. While I was at it I installed a set of OEM Nissan manual hubs that @hawairish sent my way. Much nicer kit than the Warn units I was running and they only need a 1/4 turn to engage. Gave the refurbished bumpers a quick coat of rattle can black to clean up the truck and get ready for the Southwest trip. I installed some universal mud flaps since the OE units wouldn't clear the tires to complete the look and so far they've held up really well. They come without brackets or mounting holes so it left a lot of room for interpretation but overall I think they're a great solution for my needs.
    1 point
  6. The entire cooling and belt drive system was refreshed. New radiator, pump, thermostat and housing, hoses, belts, power steering pump, alt, idlers, fan bearing bracket, fan and clutch. During my repairs I've been finding that many components, brackets, bolts etc...they're all succumbing to rust. I started ordering full sets of all bolt and nut sizes/pitches of yellow zinc JIS hardware to have on hand as I go through my truck and other projects. Additionally, i found that electrolysis is a great way to clean up super rusty parts prior to painting.
    1 point
  7. The universal sliders I've been holding onto for as long as I've lived here finally got mounted. Again, thanks to the brilliant engineering that @hawairish cooked up I mounted them via the OE locations using a set of QX4 step rail brackets and the adapter plates that he generously designed and cut out at his lab. They're robust, can easily support the weight of the truck and completely bolt-on. The truck also got a complete set of 2nd hand Coastal bumpers with a swing out that was conveniently located locally. The kit was professionally welded at a SoCal race shop so the fit up and quality was superb. Just needed a respray and some minor cosmetic repair. I bought the correct color matched silver to paint them but the window to paint outdoors here is very short and i have not managed to get the time in the 3 years since owning this set. I wasn't much of a fan of the Coastal options so I shaved most of what was on the bumper with the intention of 3D printing my own AUX/Fog light housings when the time comes around to painting them. For now its just clean and simple. An element of the Coastal design that seems pretty wild to me is the disregard for the power steering cooling line. These trucks use an aluminum tube that runs directly across the lower radiator support that the coast kit neglects, forcing users to bend it up out of the way. I opted to run a remote oil cooler next to my trans cooler and avoid what could be a disaster on the trail from a bump or collision.
    1 point
  8. The truck now has 4.6 gears. Initially I installed a SuperPacked LSD rated at 236.5 ft/lbs of breakaway that @hawairish built but after driving it for a while I found it wasn't really appropriate for my intended uses and the wet PNW environment. Would be great for a trail toy or sport truck application. So I ended up going with ARB lockers front and rear. The front hasn't made it into the truck yet but is on the bench as the next major item. The truck is already plumbed for it so I just need to finish the install into the housing and stuff it under the truck. @hawairish hooked it up with a slick bracket that he cooked up for mounting my old ARB single in the engine bay. I had originally mounted it in the rear passenger cubby and it worked well for the last 10 years in that location serving the sole purpose of inflating my tires after trail runs but with the ARB's it was time to relocate. I installed the switch panel that @hawairish and I ordered a while back that replaces the sunglass holder to run everything- Compressor, front and rear lockers, light bar, trail lights and AUX backup lights. Super stoked with the result.
    1 point
  9. Long time with no update! The truck is back from a recent trip to Moab with @hawairish and his build has inspired me to bring this thread up to speed... The truck has seen lots of trips and a handful of upgrades. Most notably is the rebuilt trans. Had some water intrusion in 2024 that prompted me to have it professionally rebuilt with a couple minor upgrades for durability and longevity. I paired that with a set of low-range gears for the transfer case that @hawairish helped make happen. Legend has it these gears are made by the same group that manufactures OEM gears but I have no proof so take that with a grain of salt. They are manufactured in Japan and have proven themselves in Moab but the install had a few hiccups that leave me curious how others have done this DIY in a garage setting. The large 4WD shaft required machining to match the OEM length otherwise it binds on the case. Not a problem as I chucked it in the lathe and made the needed modifications but unless you can machine the case or the shaft I would say this would be a show stopper. I drilled and tapped the output shaft so that I can run a SYE in the future while I had the case apart then reassembled everything and delivered it to the shop performing the rebuild so they could install everything and get the truck back up.
    1 point
  10. Falling behind on updates again... My guys' trip to Moab has come and gone, but unfortunately the truck was not ready in time for it. I still made it up there and had a great trip riding shotgun in Towndawg's truck (recently fitted with 4:1 t-case gears and a rear ARB locker...front ARB didn't get installed in time). Long story short, I was able to get the truck out of the garage and around the block a few times, but the steering and alignment didn't feel right, and the gear box started leaking. I had already rebuilt the power steering lines again (they had sprung a leak a 2nd time) so I have little confidence in their ability at the moment, but they seem to be holding now. This time around I snugged the fittings up a little less thinking maybe I was over-tightening them and compromising the liner. But frankly, if they're this sensitive to assembly, I probably don't want them. For now, they'll do. Parts are on order to rebuild the gear box, which I probably should have done in the first place. Beyond that, the setup has not been tested at all...but at least it drives now! Here were the finishing pieces of the build... The driveshaft adapter turned out great: Got the new rear 5.13 (41:8 = 5.125) gears installed. That took a lot of effort, though. I've surely mentioned it before, but the H233 used thick rings/spacers/washers of different thicknesses to set pinion height and preload, and practically all of those pieces are either no longer available, or several bucks each (and you don't really know which piece you'd need unless you have the proper setup tools). It didn't use traditional shims, and even then, there aren't really any good options available due to odd metric sizes. Fortunately, the new pinion gear sat high, so I was able to grind down OE spacer pieces on a flat belt sander. Unfortunately, it was a lot of trial-and-error to dial in the height (a lot of pressing pieces on and pulling pieces off), and I basically took the pieces down to the minimum factory dimensions to get it as close as I could. It sucked and took a lot of time, but the pattern is good. I also managed to strip some threads on the bracket that holds the actuator piston for my TJM, so I had to pull that off to weld some nuts on get some threads. I got the switches wired up for the overhead console the other week. I ran some 8-conductor wiring up the passenger A-pillar and into the engine bay. Six of the wires are for the overhead panel, and the other 2 I'll wire up for powering a USB port for the dash cam eventually. I ended up drawing ACC power, ground, and illumination from the compass module. Opened it up, soldered on leads, and crimped on terminals and harnesses. The panel is for a Patrol, and while the color isn't a perfect match for my gray "K" trim, it's close enough for me and I'm super happy to finally put it to use. Things are wired up in a way that's consistent with their usage; i.e., you can't engage the front locker unless the rear locker is engaged, and you can't engage the sway bar disconnect or rear locker until the compressor is on. Remote Air is for the tire inflation setup; it can either hold the air, deflate, or inflate. I was not able to get the compressor, relays, or solenoids wired up until last night, and tonight I needed to sort out some leaks from having to shuffle around my setup. These are not the finished pics, but close enough for now. I opted to use some modular solenoids that stack together instead of the ARB style solenoids...that 4-solenoid modular unit costs less than one ARB solenoid, but was a little tough to find. That funky rubber boot thing is an adjustable pressure sensor switch that I was hoping to use for the tire inflation (Remote Air) switch, so that it would stop inflating at a set PSI. Unfortunately, it's so sensitive that it'll just flutter at the set temperature and cause the compressor to keep cycling. So, I'll probably just retain it as a safety cut-off. Also determined tonight that gauge is garbage...it's way off. Lastly, this is how it sat as of yesterday before a powerwash. I spy something SASsy.
    1 point
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